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4-Traders Homepage  >  Equities  >  Tokyo  >  Tokyo Electric Power Company Holding Inc    9501   JP3585800000

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Tokyo Elec. Power : (Oct 26,2011)Plant Status of Fukushima Daiichi Nuclear Power Station (as of 3:00 pm, Oct. 26)

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10/26/2011 | 10:10pm CEST
*Updates are underlined

All 6 units of Fukushima Daiichi Nuclear Power Station have been shut down.

Unit 1 (Shut down)
- Explosive sound and white smoke were confirmed after the big quake 
  occurred at 3:36 pm on March 12. It was assumed to be hydrogen explosion.
- At 3:37 pm on March 25, we started injecting freshwater to the reactor 
  and are now injecting fresh water by a motor driven pump powered by the 
  off-site transmission line.
  Water is currently injected at approx. 3.8 m3/h through reactor feed 
  water system piping arrangement. 
- We commenced injection of nitrogen gas into Primary Containment Vessel at 
  1:31 am on April 7.
- At 11:22 am on August 10, we started cyclic cooling for the water in the 
  spent fuel pool by an alternative cooling equipment of the Fuel Pool 
  Cooling and Filtering System. 
- At 1:17 pm on October 26, we started cutting off the designated piping 
  after confirming that the hydrogen density inside the piping for cooling 
  in case of reactor shutdown was less than 0.1 %, as one of the 
  construction work to install gas monitoring system inside the Primary 
  Containment Vessel.

Unit 2 (Shut down)
- At approximately 6:00 am on March 15, an abnormal noise began emanating 
  from nearby Pressure Suppression Chamber and the pressure within the 
  chamber decreased. 
- At 10:10 am on March 26, we started injecting freshwater to the reactor 
  and are now injecting fresh water by a motor driven pump powered by the 
  off-site transmission line. 
- At 2:59 pm on September 14, we started injecting water to the reactor 
  through core spray system water injection piping arrangement in addition 
  to the water injection through reactor feed water system piping 
  arrangement.
- Water is currently injected at approx. 3.0m3/h through reactor feed water 
  system piping arrangement, and at approx. 7.0 m3/h through core spray 
  system water injection piping arrangement.
- At 5:21 pm on May 31, we started cyclic cooling for the water in the 
  spent fuel pool by an alternative cooling equipment of the Fuel Pool 
  Cooling and Filtering System.
- At 8:06 pm on June 28, we started injecting nitrogen gas into the Primary 
  Containment Vessel.
- At 1:05 pm on October 26, we started nitrogen purge of the designate 
  system after confirming that hydrogen is stored with the density of 6.5 % 
  when connecting piping arrangements on October 20, 2011, as one of the 
  construction work to install gas monitoring system inside the Primary 
  Containment Vessel. We finished the nitrogen purge at 1:42 pm because we 
  confirmed that the hydrogen density was 0%.

Unit 3 (Shut down)
- Explosive sound and white smoke were confirmed at approximately 11:01 am 
  on March 14. It was assumed to be hydrogen explosion.
- At 6:02 pm on March 25, we started injecting fresh water to the reactor 
  and are now injecting fresh water by a motor driven pump powered by the 
  off-site transmission line.
- At 2:58 pm on September 1, we started water injection by core spray 
  system in addition to water injection by the reactor feed water system 
  piping arrangement. 
  Water is currently injected at approx. 2.0 m3/h through reactor feed 
  water system piping arrangement, and at approx. 8.1 m3/h through core 
  spray system water injection piping arrangement.
- At 7:47 pm on June 30, we started cyclic cooling for the water in the 
  spent fuel pool by an alternative cooling equipment of the Fuel Pool 
  Cooling and Filtering System.
- At 8:01 pm on July 14, injection of nitrogen gas into the Primary 
  Containment Vessel started.

Unit 4 (Outage due to regular inspection)
- At around 6 am on March 15, we confirmed the explosive sound and the 
  sustained damage around the 5th floor rooftop area of Reactor Building.
- At 12:44 pm on July 31, we started cyclic cooling for the water in the 
  spent fuel pool by an alternative cooling equipment of the Fuel Pool 
  Cooling and Filtering System. 
- At 11:34 am on August 20, we started an operation of desalination 
  equipment in the spent fuel pool.
- At this moment, we don't think there is any reactor coolant leakage 
  inside the primary containment vessel.

Unit 5 (Outage due to regular inspection)
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 5:00 am on March 19, we started the Residual Heat Removal System Pump 
  in order to cool the spent fuel pool.
- At 2:30 pm on March 20, the reactor achieved cold shutdown.
- At 2:45 pm on July 15, we started the operation of the original Residual 
  Heat Removal System (System B) by its original seawater pump.
- At this time, we don't think there is any reactor coolant leakage inside 
  the primary containment vessel.

Unit 6 (Outage due to regular inspection)
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 10:14 pm on March 19, we started the Residual Heat Removal System Pump 
  of Unit 6 to cool down Spent Fuel Pool.
- At 7:27 pm on March 20, the reactor achieved cold shutdown. 
- At 2:33 pm on September 15, we started separately cooling the reactor 
  through the Residual Heat Removal System and the spent fuel pool through 
  Equipment Cooling Water System and Fuel Pool Cooling System.
- At this time, we don't think there is any reactor coolant leakage inside 
  the primary containment vessel. 

Others
- At around 10 am on June 13, we started the operation of the circulating 
  seawater purification facility installed at the screen area of Unit 2 and 
  3.
- At 8 pm on June 17, we started operation of Water Treatment Facility 
  against the accumulated water. At 6:00 pm on July 2, we started the 
  circulating injection cooling to inject the water, which was treated by 
  the accumulated water treatment system, to the reactors through the 
  buffer tank.
- At 7:41 pm on August 19, we started treatment of accumulated water by 
  parallel operation of one line from the cesium adsorption instrument to 
  the decontamination instrument and the other treatment line of the cesium 
  adsorption instrument No.2. 
- At 2:06 pm on October 7, we started to spray purified accumulated water 
  brought from Unit 5 and 6 continually in order to prevent dust scattering 
  and potential fire outbreaks from the cut down trees.
- At 10:00 am on October 20, we started transferring the accumulated water 
  from the basement of turbine building of Unit 3 to the High Temperature 
  Incinerator Building of Central Radioactive Waste Treatment Facility.
- At 10:12 am on October 20, we started transferring the accumulated water 
  from the basement of turbine building of Unit 2 to the Process Main 
  Building of Central Radioactive Waste Treatment Facility.
- From 5:31 pm on October 25 to 2:01 pm on October 26, we transferred the 
  accumulated water brought from the basement of turbine building of Unit 1 
  to the basement of turbine building of Unit 2. 
- At 10:00 am on October 26, we started transferring the accumulated water 
  from the basement of turbine building of Unit 6 to the temporary tanks. 
- At 9:47 am on October 26, for the water injection to the reactors of 
  Units 1 to 3, we switched from normal water injection line to emergency 
  water injection line, due to the shutoff of facilities for power source 
  reinforcement work. Along with the switching work, we adjusted the amount 
  of water injection from water feeding system to approximately 3.8 m3/h 
  for Unit 1's reactor. Likewise, we adjusted the amount of water injection 
  to Unit 2's reactor to approximately 3 m3/h from water feeding system, 
  and to approximately 8m3/h from Core Spray System.
- On October 26, we replaced the vane to adjust flow amount of water 
  injection line to the Unit 3's reactor in order to improve the ability to 
  control the water injection amount. 

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Financials ( JPY)
Sales 2018 5 675 990 M
EBIT 2018 -
Net income 2018 267 670 M
Debt 2018 5 113 389 M
Yield 2018 -
P/E ratio 2018 2,76
P/E ratio 2019 3,99
EV / Sales 2018 1,03x
EV / Sales 2019 0,96x
Capitalization 740 835 M
Chart TOKYO ELECTRIC POWER COMPA
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Tokyo Electric Power Compa Technical Analysis Chart | 9501 | JP3585800000 | 4-Traders
Technical analysis trends TOKYO ELECTRIC POWER COMPA
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Income Statement Evolution
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Mean consensus HOLD
Number of Analysts 4
Average target price 487  JPY
Spread / Average Target 5,6%
EPS Revisions
Managers
NameTitle
Tomoaki Kobayakawa President & Director
Takashi Kawamura Chairman
Toshihiro Sano Director
Yuji Masuda Director
Toshiro Takebe Director
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